Everything posted by SergeyPe
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TM TCA Boeing Yoke Roll Axis Sensor Upgrade
Hello alex40. Although I had an Alpha some time ago, I've never compared the deadzones in these two yokes.
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more Winwing Hardware news
Totally agree- the quality is very good (and the price is amazing 😁).
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more Winwing Hardware news
Oh... silly me. It's just that WinWing has just launched the 737 EFIS and I was discussing this matter with a colleague on a different forum... Sorry.
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more Winwing Hardware news
Just my five cents... There are no EFIS L and R units. There are "N" modules for the 737 NG and "M" modules for the 737 MAX as described quite clearly on WinWing website. So to get a full set (with MCP) you need to buy two identical "N" or "M" modules, depending on the 737 version they'll be used with. However on the well-known photo from WinWing both versions are shown as L and R EFIS modules, so the resellers are actively offering "N" as a Captain and "M" as a Co-Pilot modules. No comment...
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Fulcrum One Yoke problem
Great! The symptoms you've described were clearly pointing to a mechanical slippage; I'm happy to be able to help 😀. As for the sensor difference- I have one of the early yoke designs and based on the discussions with Chris I know that he made quite a number of changes in later versions, including the sensor types.
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Fulcrum One Yoke problem
Sure, done in the same Mega folder. Unfortunately I've replaced the stock sensors for the different ones already some time ago, so the close-up pictures of the original design are not available. However the new sensors have a similar design so I've added another picture where the sensor shaft/ back plug linkage is visible. Please note some copper foil I had to wrap around the sensor shaft to ensure the snug fit. Check that there is no slippage of the sensor shaft against the back plug when the yoke handle is rotated. Make a mark somewhere on the sensor shaft to simplify the task. It might also happen that the sensor itself is not fixed firmly to the mounting bracket with a nut so that the sensor body is rotating against the bracket (which seems a bit less likely).
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Fulcrum One Yoke problem
What I would check first is the mechanical linkage between the tube and the roll sensor shaft. It sounds like the sensor shaft is slipping slightly against the tube's back plug so that the tube rotation is not translated to the sensor within a 90 degrees range from the center to a full anti-clockwise position. This would provide exactly the symptoms that you are describing. This applies to the first version of the yoke with TT6120 sensors (the black ones as on my photos).
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TM TCA Boeing Yoke Roll Axis Sensor Upgrade
OK, I've checked the roll deadzone on my TCA Yoke. If measured at the outmost of the yoke handle it's about 5 mm in total which IMHO is quite OK. I wonder what's the result on your unit? BTW- a dumb question: are you getting a big deadzone both in the sim and in the testing program? Typically the deadzones for all the axes are set quite big by default in all the sims. I've also checked TM Target- the deadzones there are set to 0 by default for TCA Yoke, so it won't help.
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TM TCA Boeing Yoke Roll Axis Sensor Upgrade
Hi @TomaszBartchie and welcome to the club! Honestly speaking, I haven't checked the deadzone difference after changing the sensor, also because the TCA Yoke is not my main one- I am usually flying with a Fulcrum (heavily modified), which in my opinion is well ahead of any other non-feedback yokes in the market. It might well be that TM used a deadzone to cope with a non-linearity of AH49 which is most sensitive around the center position. One thing that comes into my mind is that the possibility of adjusting the response curves to reduce the deadzone is built into TM Target software (if I am not mistaken, as I didn't use Target for quite a long time). Please give me some time to pick the yoke out of storage and play with Target- I'll be back with the results.
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Winwing PAP3 (MCP) Aircraft Support?
WinWing website product page -> "Applicability" -> "Continuous Updates for Aircraft Compatibility" -> "Click to Check the Latest Update".
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WinWing MCDU AND CDU'S. They look Good.
On this page go down to a "Record-breaking, dual-mode display drive" picture and there you'll see the "MCDU Platform Compatibility Schedule" with a "Click to view details" box.
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Gladiator NXT EVO flight stick. Cheap. Outstanding.
No they don't, and AFAIK they are not planning it. The metal grip (MCG Ultimate) is a 95-% replica of a real one which is used in SU-57 fighter; they didn't want to spoil the realism😀. Well, almost, as the real-life grip is plastic, not metal, but after the success of the plastic version (MCG/ MCG Pro) the demand for the metal one was high (inspired by the Thrustmaster cougar/ Warthog/ F-18). The SCG, on the contrary, was aimed at a much wider range of simulators, including the space ones- hence both the right-hand and the left-hand ones were available from the start of production.
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FSLabs A320 for P3D- aviaCDU shows a black screen
As said in the title- when trying to connect, the message pops up: "Connected to: A320 L (or R) MCDU" and then the screen goes black. It works fine with all the other aviaCDU's I have licensed (Aerosoft A320, PMDG etc.). Prepar 3Dv4, aviaSERVER v19.2.4.0. Any suggestions on why it happens?
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Gladiator NXT EVO flight stick. Cheap. Outstanding.
"High grade" are the key words here; and BTW, Warthog gimbal is all-plastic of much worse quality which is prone to breaking with heavy use...
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TM TCA Boeing Yoke Roll Axis Sensor Upgrade
Hi! 1. The calibration is explained in the AS5600 datasheet (Page 23- Angle Programming Through the OUT Pin). Please note that in addition to the red jumper that you can see on my pictures #7 and #8 you'll also need to connect the two upper leftmost contacts on the PCB to set the output voltage increase with a magnet clockwise rotation (I've just put a drop of solder there). The wire loop that can be seen on the pics is connecting the PGO pin to the ground to put the chip into programming mode; it should be cut off after the calibration. 2. I used PETG, but PLA or ABS will do as well. Regards, Sergey
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Button stuck down.
Any similar-sized button will do, providing that it's of a momentary-switch type.
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TM TCA Boeing Yoke Roll Axis Sensor Upgrade
Yep; actually your post was one of those triggering my investigation- thanks for that!😀.
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TM TCA Boeing Yoke Roll Axis Sensor Upgrade
After having acquired my own TCA yoke I decided to investigate the reason for the roll axis issues reported by some of the users. The first thing to check was the roll axis sensor as some of the users were reporting a strange dependency of sensor operation on the external magnetic field (which shouldn't be the case with a properly designed sensor). So after the disassembly I was very much surprised to see the roll axis sensor to be designed around a single AH49E chip which is a simple "old-style" analog Hall-effect sensor. There is a couple of issues with this solution: 1. AH49E is reacting to a magnetic field strength variation in any direction relative to it's body. When a small round diametral- magnetized magnet is rotated close to it, the field strength change is non-linear in relation to the rotation angle. Which means that the yoke's reaction to roll axis rotation is stronger near the center and becomes weaker close to the rotation extremes. Of course it can be compensated in the sim by choosing a non-linear response curve, but in my opinion having a sensor with a non-linear response and no internal compensation for it is simply not right. 2. The magnet is not too strong, so the output signal swing for a full side-to-side yoke rotation is mush less than a sensor power supply voltage. When the yoke internal calibration is performed, the signal is- well- 'amplified" digitally within a yoke controller to match the controller's reference signal voltage swing (from 0 to full power supply voltage). Unfortunately any "noise" (magnetic or electric) that might be induced to the sensor circuit/ connecting wires (that are quite long) will be amplified as well increasing the roll axis sensitivity to the external interference. 3. As AH49E is sensing any changes in the adjacent magnetic field strength, any external ferromagnet object near the back of the yoke handle will create a disturbance in the roll axis; the same goes for the stability of the internal magnet. In some cases this might require a yoke re-calibration. My solution to this issue is the replacement of a simple Hall-effect sensor by a different type specifically designed for registering an axis rotation. In my opinion the best DIY option here is AS5600 from AMS. The main features of the chip are: 1. It is reacting to a degree of magnetic field rotation in relation to a chip's upper/ lower cover. The signal is directly proportional to the rotation angle with a very good linearity. 2. AS5600 offers a very simple internal calibration routine which adjusts the sensor's output signal swing (from 0 to power supply voltage) to a full rotational angle required. This means a much better immunity to the external "noise". 3. AS5600 is not sensitive to the magnetic field strength variations so the external ferromagnet objects do not influence the sensor operation. Also there is no need of a periodic yoke re-calibration. In practical terms the option that I've chosen was to use the ready-made AS5600 board available from Amazon or eBay (also from AliExpress). It has all the external elements needed and the size allows to fit the board into the existing opening in the roll sensor base without the need of any mechanical trimming of either the sensor or the base. The board requires soldering one additional jumper to set the correct power supply voltage. Here is the set of pictures showing the mod. After removing the existing sensor and mounting the new board the new sensor needs to be calibrated internally but it's a very simple procedure not requiring any additional tools. Having done the mod I'm quite happy with the results. If any of you are interested, I'll be happy to provide the additional details.
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Button stuck down.
Great, Ray! You are more than welcome😀. I'm also happy to hear that Chris is active with the recovery plans; he really deserves every bit of success in that!
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Button stuck down.
Please convey the same wishes and hope from me as well.
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Button stuck down.
I'd expect that most of the smaller British companies would be sourcing the parts from the same big guys like Mouser or Digi-Key- it's probably cheaper than investing in their own local stocks...
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Button stuck down.
OK, excellent idea! I'll put it together tomorrow.
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Button stuck down.
Actually there are three cap types fitting the yoke switches; they differ by the cap diameter: 70890 is 0.2 inches (5.08 mm), 75270 is 0.375 inches (9.53 mm) and 80180 is 0.310 inches (7.87 mm). 80180's are actually used on the Fulcrum. You can download the datasheet from the same Digikey link, it has all the information about the switches. And just in case someone else needs this info (hopefully not😀)- the trim switches are C&K 7105, the hat switch- ALPS RKJXM (actually Chris used the kit from Leo Bodnar).
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Button stuck down.
Yes, it's the correct part; hopefully you'll get the yoke fixed fast. If any other questions pop up, don't hesitate to ask😀.
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Button stuck down.
😀😀😀 I'd be very much surprised if he hasn't- these are the biggest electronic parts suppliers operating worldwide; in the UK for sure. And C&K 8020 series is widely used in various kinds of electronic equipment- shouldn't be a problem to get one. BTW, there is another option, which is Salecom P8701. It's a cheaper 8125 Chinese clone of quite a good quality, but it's tactile "click" is slightly different from C&K, so I'd advise an original one.